Thursday, March 29, 2007

Fixing the Transmission

Well, these pictures are a little late, but here they are. I spent most of last week replacing the broken parts in the transmission.


Here are the two replacement bearings from Pelican Parts ($400!) that I pushed into the transmission intermediate plate after heating it up with the orange heat gun to the left.
They went in surprisingly easy.


Here are the new synchro rings to fix the grinding 1st/2nd gears. They are $65 apiece and have a special molybdenum coating for proper friction during shifting.


I removed the snap rings from 1st, 2nd and 3rd gear to replace the synchro rings.


Here we are torquing down the 12-point nuts that hold the bearing shield in place. This is the same 12-point tool that I used to remove the CV joints under the car.


Here is a badly worn 1st gear synchro ring. if you click on the picture and look at the cross-section on the left, you'll see the bottom edge very worn down. No wonder 1st and 2nd gear were grinding!


Here are the two transmission shafts inserted into the intermediate plate. There were too many parts to hold, so I had to wait for my friend Rick to come over (while on a date, no less) and hold this assembly together while I hammered on the inner race pieces for the shaft bearings.


Here is the gear assembly with all shafts, shifting rods and gears in place.


I'm almost ready to put these two pieces back together; however, there are still old gaskets on the transmission edges and I have to scrape those off first.

Tuesday, March 27, 2007

AC Motor Controller Installed


Tim, happy to get the controller installed


A closer view of the Azure Dynamics AC motor controller.

After purchasing hardware from Home Depot to install the controller plate, I came home and drilled all the required holes for the mounting bolts. After squirting all the aluminum and metal caulk around the plate, I realized that I couldn't tighten any of the bolts myself because one end was on top of the car and the nuts were under the car. Big thanks to my friend John for coming over on short notice to help me tighten the bolts before the caulking dried. I'll try to be better prepared next time.

Also, notice the larger, two-inch, holes cut in the trunk floor and wall to the left of the controller. The control and motor cables will route through these holes.

Next up: getting transmission parts delivered and putting the transmission back together.

Monday, March 26, 2007

The First Sawzall Cut for the Controller Plate


My first use of a Sawz-All. The hole for the motor controller plate.


All the transmission pieces (waiting for new parts) covered up to prevent metal shavings from getting into them.


The motor controller plate provided by ElectroAuto before being bolted and caulked in.

Today I got to try out my new set of cobalt metal-cutting drills and the SawzAll I borrowed from my dad. Both worked quite well and cut through the steel floor of the rear trunk like butter. I botched the hole rather badly, going outside the lines by an eighth inch in some places, but things should still work. My drill ran out of battery charge so I'll drill the bolt holes tomorrow after getting hardware and caulking from Home Depot.

The directions say to not cut the transmission ground bolt, but move it if you have to. I did cut the bolt off and will have to install a new one. I suppose I could have hammered the front edge of the controller plate hole flat, but installing a new transmission bolt will be much easier.

Sunday, March 25, 2007

A few measurements to not forget...

While taking apart the transmission, I took some measurements with a digital caliper. These are probably different from other 914s out there, but I wanted to record them here in case I lose them amid the rapidly increasing paperwork.

Distance from edge of flywheel to engine housing: 1.684-1.687 inches at various places

motor adapter cone depth: 1.318 inches

motor adapter socket depth: 1.373 inches

4th/5th gear shift fork to bracket on shift rod: 0.127 inches

2nd/3rd gear shift fork to ridge on shift rod: 0.202 inches

Cheers!

Saturday, March 24, 2007

Transmission Woes (More than I bargained for)

Today was an educational and humbling day. I appreciated having the new garage space after the engine went away. I started opening up the transmission because first and second gears were grinding badly and I wanted to see if I could replace the synchro rings.


Here's the back end of the transmission with the cap removed. The crescent-shaped shifting fork for first and reverse is on the left. The expansion bolt with the golden speedometer gear is in the center.


Here's the back end of the transmission. When I pulled off the back end, the reverse gear in the upper left fell out with all its various pieces all over the floor. I'll try to not do that again.


Here's a closeup of the first/reverse gear shifting fork. I took this so I could align the fork when I put the transmission back together.


Here's the synchro ring (just above the small teeth) for first gear. As I suspected, it's clearly worn down and probably not doing much any more.


To continue taking apart the transmission, I needed to remove the shift-lever fingers which activate the internal shift rods.


I also had to remove the reverse gear electrical switch pin (which goes in the small hole).


Here's the back of the transmission with the intermediate plate removed and all the gears pulled out. The large top hole at the back comes from the driveshaft and the larger hole in the center goes to the differential.

On a side note, the transmission was covered with grease and, after removing the clutch throw-out arm, that there's a major leak in the transmission drive-shaft seal.


Here's the intermediate plate with all the internal gears still attached.


The same assembly turned over to reveal the golden shifting forks for 2nd/3rd gear and 4th/5th gear.


To get the gear shafts out, I had to remove the forks and the three shifting rods, shown at the top.

Oh, the horror! If you click on the picture above and zoom in on the right bearing, you'll notice that its cracked apart in several places. These bearings go for at least $185 at Pelican Parts, more elsewhere.


Oh, more horror! The pile of bearing parts and balls fell out of the driveshaft gearset when I removed it. This bearing costs over $200. I hope I didn't cause these failures when tapping the transmission shafts to get them out. I would think it would take much more force than that.


I was able to shake the gears and pieces loose from the pinion shaft and line them up on a 2x4 for inspection.


The synchro ring for third gear has significant wear, but is still marginally useable.


As I suspected, the synchro ring for second gear is completely worn down and useless, causing nasty gear grinding. These synchro rings are reasonably easy to replace but cost about $65 each.


Here are the balls and broken pieces from the broken pinion bearing inside the intermediate plate. Again, I hope I didn't cause this breakage. The inner race piece that rubs against this bearing on both sides is a bit tight on the shaft and I'll probably use heat to put them back on the shaft to prevent future breakage.

Again, this was a fun day with several runs to the store for obscure tools (like a ring spreader and a gear puller), but overall it was educational. I'm probably back about $600 in transmission parts just to put the transmission back together, but they needed replacing anyway. I'll have Alan over at A & P heat up the intermediate plate and replace the two broken bearings.

Next up: cutting the hole for the motor controller box...

UPDATE: I did a much closer examination of the broken bearings and the broken edges all had significant wear since they were broken, indicating that they've been bad for quite a while. Leave it to German engineering to keep things running past their time.

After ordering all the broken bearings, seals, synchro rings and such, the total bill at Pelican Parts (with a $20 discount they sent me) was..... $620.00 (Ugh!). I guess I'm a stickler for a good stickshift. On a more positive note, I was washing the intermediate plate in hot water and it heated up enough that the broken bearing sleeves just popped right out. I might not need to spend the $$$ at A & P to have the new ones installed if they are just like the old ones.

Make it go away! (The engine, I mean)

This morning, Jamie from Corvallis bought my engine and took it away, freeing up much needed garage space. Thanks, Jamie!


Engine in Jamie's van with a bunch of extra parts.


Me, enjoying my desperately needed garage space.

Friday, March 23, 2007

A Cheap Balancer and Transmission Issues



After talking with some engineers at HP and mulling over some ideas, I came up with the attached schematics for an inexpensive battery balancer. This one relies much more heavily on complex PIC programming and uses an off-the-shelf laptop or inkjet-printer power supply to deliver an isolated source of power for the battery charger. Any feedback you have is welcome. The analog engineers at work are still designing the current/voltage limited step-down buck converter so that will be coming when I get their feedback.

On a different note, I called Alan at A & P today to see how much it would take to rebuild the removed transmission. 1st and 2nd gear are grinding badly and I think the synchro rings are gone. His response was approximately $500 in labor and $800 in parts (OUCH!!!).

I'm going to try to replace the sychro rings myself based on the Pelican Parts article and, if I screw up, I'll take the whole thing back to A & P to put it back together. What's the worst thing that could happen :).

Wednesday, March 21, 2007

More Thoughts on Battery Equalization

Lee Hart, an EV guru on battery maintenance and equalization, has graciously e-mailed with me regarding the best way to equalize batteries. He's currently working on upgrading his battery balancer (see link at right) to handle a wider range of battery technologies and applications.

Lee convinced me that the flying capacitor approach that I originally thought would work is not practical in real world situations. I think Lee's battery balancer design would do a great job; however, I'd like to cost reduce it to something more suited to my own needs.

My plan is to create a relay board like Lee's that only handles 10 amps per relay instead of 30. If I costed out the parts and boards correctly, I can probably get that down to $100 per relay board vs. Lee's assembled cost of around $200. For the main controller board, I plan to use a similar design, but simplify the design to meet a narrower set of needs and replace the high-cost components with lower-cost, harder to use components.

For example, instead of a $80 complex STAMP controller, I'll use a $6 PIC that has more flexibility but will require more complex programming. Instead of the $150 Vicor BatMOD module, I'm using a free 100-watt 32-volt isolated power supply from an HP printer and making a current controlled buck converter to step down the voltage and charge the batteries (about $10). Instead of the $60 Radio-Shack meter, Lee is working on using an LM331 voltage to frequency converter to measure voltage and current of the charger which should cost around $10.

Many of these components will be harder to calibrate and program, but I'm willing to do that to lower the cost and reduce the size of the system. I don't know how this will end up, but I'll learn a lot and that's the point.

Flywheel and Engine Mount Removal

I put the engine for sale on CraigsList and have to prepare it for delivery this weekend. There is very little space in my one-car garage so getting rid of the engine while keeping all the necessary components will be good.

In order to get a last measurement of the flywheel to housing distance, I got a digital caliper from Harbor Freight Tools for only $29. It's remarkably accurate down to .001 inches and is very easy to use.

I chatted with a local Porsche enthusiast named Pat and he let me borrow the tool on top which is a flywheel lock to hold the flywheel still while I undo the heavily torqued bolts. Thanks, Pat!


I've already removed the clutch assembly and here's the face of the flywheel. Note the long breaker bar and flywheel lock needed to remove the the flywheel. With these tools, the job was a total snap and only took me a few minutes.


Here's the end of the engine case with the flywheel removed. I was surprised by how gritty the flywheel bolts were after they came out.


Next up was removing the front engine mount. The engine was balanced on one end of the furniture dolly, so I used the floor jack to raise the front end. I was able to raise the engine far enough to drop off the unbolted engine mount and support the engine with a 2x4 instead.


Here's the removed engine mount ready to be used in the EV conversion. Jamie from Corvallis (who knows Otmar and his 914 EV - see link at right) may drop by this weekend to pick up the engine and help me free up some much needed garage space.

Ugh, it's late and I'm going to bed.

Tuesday, March 20, 2007

Transmission Removed!

This was a big evening of figuring out how to remove the transmission with one person.


First up was removing the rear portion of the exhaust system, shown here next to my trusty 34mpg 1994 Saturn. (Someone else converted a '94 Saturn Wagon to an EV, but I'll keep mine!)


Here is the removed transmission. I'll try to take more pictures as I go next time to document the process better. Notice the 2x4 blocks on the ground to hold up the transmission so that it doesn't stress the driveshaft with the bolts removed.


After removing the exhaust, I slid the engine over on the furniture dolly so all the transmission points were on blocks outside the dolly. Note the stack of 2x4s on the right edge of the picture to hold up the transmission half of the engine.


Here's the removed transmission on the ground. The inside is covered with black grease. I wonder if there's a leak somewhere. Note that there are still plastic bags covering the transaxle openings that connect to the CV joints.


Interestingly enough, there was a "plug" of something that filled in this notch in the bottom of the transmission. I'm not sure why it was there.


Here's the engine half of the two pieces. The clutch looks darn near brand new with very little wear. I'm selling the engine to someone in Corvallis and they'll get this great clutch since I've already purchased a new one as a replacement. My only concern is that I'll be taking the flywheel for the EV conversion. That'll knock off a buck or two off the selling price.

Again, note the two transmission bolts at the bottom of the flywheel jutting out and the stack of 2x4s to hold up the transmission so it's removal doesn't stress the driveshaft.


Acutally, the first thing out, even before the exhaust, was the starter motor.


For storage of the transmission, I supported it on blocks to prevent the clutch pulley, shift linkage case and speedometer connection from supporting any weight.

I looked at possibilities for removing the front motor mount on the engine that I'll need for the conversion, but it's looking rather nasty.

Next up: Clutch and flywheel removal. I might need to get a flywheel removal block to keep the crankshaft from turning to do this.

Monday, March 19, 2007

More engine drop pictures

Blogger just took me off of "spam blog" status, so I can now post more pictures of the engine drop procedure.

Here are some 2x4s under the chassis to prevent the car from coming down.


I also put 4x4 blocks under the axles to prevent the brake shields from getting damaged in case I lowered the body too much.



Here's the primary engine mount after I unbolted it. This was a royal pain because I had to hold the nut on the top of the mount to keep it from spinning in place and there's not much room to maneuver in there.


Here is the removed transmission mount with its two brackets at the top edge of the picture. The engine drop instructions specifically say to remove the entire mount instead of just unbolting the center.


A common problem when dropping the engine is to get one of the CV joints caught under the starter motor like this. I had to move the engine to the right and lower the body a bit to get this unstuck.



The left CV joint is now free and sitting on top of the engine.


In order to hold the car up high enough, you need the tallest six-ton jackstands you can get your hands on.


Here's a final shot, specifically focussing on the transmission since it's really the only piece I'm going to keep of this beast.

Cheers!

Friday, March 16, 2007

blogger issues and engine drop picture


Apparently Blogger thinks this blog is a spam site and is forcing me to type in characters with each post. This wouldn't bother me, except that it doesn't accept my character input as valid, even though I've tried a few times. I've put in a request to stop this, but it will probably take awhile. In the meantime, I've pulled out the engine and rotated it for easier access to remove the transmission.

More parts but no instructions or hardware...


This week has been a whirlwind and I haven't caught up on sharing all the pictures. Last Tuesday, I received another shipment from ElectroAuto. This one included the motor controller mounting plate (large black rectangle), its rubber mounting posts and the potbox and its mounting plates. Since this kit is the 914 AC kit, I have no idea how to install the controller plate. In addition, ElectroAuto hasn't sent any hardware (specifically the rivnuts) so I can install many of these pieces.

I've contacted Randy Pollock, the first person to order a 914 AC kit and he and I are working to figure this out. Randy has been gracious enough to help ElectroAuto with installation instructions, photos and other descriptions.

On another front, I'm rapidly running out of space in my house and single-car garage for storing pieces that I've removed from the car. I ran out to Camp914 today to drop off the old suspension and fuel tank with Craig so he can sell the parts and possibly donate to the electric car project.

I'll post more pictures of the engine drop soon, but I'm possibly climbing Mt. St. Helens tomorrow and have to finish packing. More soon! Cheers.

Tuesday, March 13, 2007

Dropping the Engine


The engine just about a foot below mounting height.


Engine pulled back about a foot.


Hole left over in the engine compartment with dropped engine.
Notice the belt that drives the air pump for the emission control system.


Well, I worked for the last three hours to drop the engine out of the car. I followed all the directions in the Pelican Parts technical article and didn't miss any attached parts. After several expletives and tense moments under the car, the engine finally plopped down onto the furniture dolly.

The article mentioned that there was very little clearance for the fuel injectors. That was actually an understatement. There was negative clearance and I had to bend the flexible fuel hoses to the injectors just to clear the sheet metal. Removing the rubber stripping was definitely a huge help.

I'm surprised by how big the engine is relative to the transmission. With the engine and exhaust system gone, there will be loads of room for batteries. I'll be psyched to sell the engine on Craiglist and get that gas-burner out of my garage...

I took loads of pictures and will post most of them tomorrow, but I'm just too tired right now to process and document all the images. So here's a few above.

Sunday, March 11, 2007

Days 3 and 4




I spent yesterday (Saturday) disconnecting all the cables from under the car in preparation to drop the engine. The shift linkage was especially hard because it moved around so much. My friend John (above) held the shift lever still while I yanked out the linkage earlier today. I also drained all the engine oil and transmission fluid. My buddy Pete is providing some 2x4s later today to hold up the car so I can drop the engine this week.

Yesterday was a bummer because I got really sick. I suspect I got stuck in the closed garage with all the fumes from the fuel system sitting out on the floor. Having transmission fluid dumped on my shoulder also stunk wretchedly. I got so sick, I vomitted twice. After completely airing out the house and a good night's rest, I feel much better today.

My biggest concern now is blazing through all this work only to have to wait for more parts from Electro Automotive to continue. In the meantime, I'm going to be working with Lee Hart on an improved battery balancing system (see link to the right). Lee is well known in the EV community for making practical, effective circuits for EV owners. I feel privileged to work with him (even if he does use a ten year old DOS copy of Orcad to design his circuits :)

Friday, March 9, 2007

End of Day 2

Most of today was spent just taking the car apart. My friend Pete came over for lunch and we removed the front and rear trunk lids. We also drained the fuel tank by operating the fuel pump with a 12V gelpack battery and took out the fuel tank. I even went so far as to yank out all the fuel lines that go down the center tunnel of the car. There's no going back to gasoline now!

I continued to spend most of the evening disconnecting cables, hoses and wires to allow the engine to be removed from the car. I didn't have the proper tool to disconnect the shifting linkage, so that will have to wait until tomorrow. Craigs 12-point tool for removing the CV joints worked like a charm.

Big thanks to Pelican Parts for their technical article on how to easily drop an engine:

http://www.pelicanparts.com/techarticles/914_engine_drop/914_engine_drop.htm



Pete helping me remove the fuel system and front/rear trunk lids.

Fuel compartment without fuel tank.


The empty fuel tank with separated expansion tank (to remove the fuel guage plug).
Note the two hydraulic jacks near the wall. Having two jacks makes dropping the engine much easier.


Rear trunk lid removed.


Method of connecting 12-volt gel-cell to fuel pump to dump fuel into gas can.


The front and rear trunk lids, removed.


The car jacked up and held with a hydraulic jack and two jack-stands per side.


An unseparated CV joint with two 12-point bolts showing.


The CV joint separated and protected with a plastic bag.

I'm covered with grease and looking forward to a good night's sleep.

Thursday, March 8, 2007

Hanging out with the OEVA folks

In addition to starting the conversion, the OEVA had their monthly meeting this evening. I got to chat with a bunch of folks about battery management systems and share my excitement over starting the 914EV conversion.


Keith on his all-electric scooter


Demonstration of a battery equalization system that uses one charger per battery after the main charger finishes with the bulk charge.

Whew, what a day. I'm going to bed now.

Day 1

Here is some progress in the first two hours:

Covering wrenches with blue electrical tape for battery work.


Removing the Engine Cover


Taking out the Battery


Removing the starter wire from the positive battery terminal


Uncovering the fuel pump for draining gasoline


Taking out the "classic" WoooGaaa horn

The next step will be to take off the front and rear hood lids, which I'll need an assistant.

The desulfation experiment continues

On a more process-oriented note, the 8-volt battery sitting on the desulfator is up to 9.1 volts (from 7.95 volts), so I have warm fuzzies that the desulfation system is working somewhat. I'll wait until the battery gets up to 9.6 volts (float voltage) and see what the specific gravity is. If this experiment works, I might splurge and purchase a $500 super-desulfator and offer to desulfate batteries for the OEVA club. The super-desulfator is 25 times as powerful as the one I have now and should desulfate a 70 pound battery in three days (whoosh!).

On the battery equalization front, I got some feedback regarding the flying capacitor circuit that I presented in a prior blog entry. While the flying capacitor approach is elegant and simple, it just isn't effective in a practical system because very little charge is transferred as the voltage on the batteries approach each other. A more effective system was designed by Lee Hart. The schematics and other info is located at the following link:

http://www.geocities.com/sorefeets/balancerland/index.htm

The major drawback of Lee's system is that it's expensive. The OEVA club is looking into this and I hope to cost reduce the system to be only $20 per battery. Perhaps using a PIC microcontroller and slightly lower currents will help. My engineering buddies are looking into this now.

Let the Conversion.... Begin!

I just got back from A & P Specialties where Alan replaced the suspension on the 914 and did a steam cleaning in the engine compartment. Without the battery weight and having the unaligned suspension, the car rides unstable and high. No matter, I'm going to start preparing to drop the engine this weekend. I ran out and got another floor jack and a water-proof label-maker so I can mark all the wires and hoses as I take them out.

Today is the last day I will drive the 914 as a gasoline vehicle. With the busy-ness of life and the delivery delays from ElectroAutomotive, I don't know how long this will take. This will be an exciting process for sure. I feel grateful to have an army of supportive friends, OEVA members, and engineers at HP all backing me up.

Damn The Torpedos - Full Speed Ahead!

Saturday, March 3, 2007

The Great Desulfation Experiment




Can one revive a mostly dead battery? Several internet sources say yes. Above is a picture of a heavily sulfated 8-volt golf-cart battery I acquired yesterday. It had a floating voltage of 7.85 when I got it and needed half a gallon of distilled water to fill it back up. Just off to the right of the battery I've attached the $250 "Cadillac of Desulfators" and it's merrily buzzing away along with a 1-amp trickle charger. At the end of today, I measured a charging voltage of 8.36 volts which should go up over time if the battery desulfates.

Don Denhardt, the national desulfation mastermind claims that this desulfation unit will restore one pound of sulfated battery per day. With the battery weighing in at about 70 pounds, this will take awhile, but I think it's worth trying to see if desulfators are worth it. Of course, the battery could have shorted plates and other problems that desulfation won't fix, but I'm going to give it a shot.

I still have two other 8-volt batteries (top picture) that I cleaned up today that also needed about half a gallon of water to fill each. They also started around 7.65 or 7.70 floating voltage so maybe I'll try to revive those too if this one shows promise. I suspect that I won't actually use these batteries in the 914 EV, but this research will help me understand battery technology better and perhaps give me some backup batteries in case one or two original cells go out. Who knows, I might even be able to revive bad cells in the battery pack if this works. Let's cross our fingers.

Friday, March 2, 2007

Getting Old Batteries and Fixing the VDO Clock




Whew, today was a long day. My friend Jonathan was in town and helped me go out to pick up some old, sulfated 8-volt batteries from Pacific NW Yamaha Golf Cars. Bob at NW Yamaha was great and sold me some old 8-volt batteries for $5 apiece. I'm going to use these to test out my 8-volt desulfator system to see if I can revive them. These US-Battery models are the same that are going into the electric car conversion. The one on the bench in the picture above was rather low and I had to add half a gallon of distilled water to fill it up.

Jonathan and I also headed back out to Camp914 to say HI to Craig and get some 914 counseling on how to jack up the car and remove the engine. He graciously let me borrow his special "12-point CV joint removal tool" (pictured above) so I could disconnect the engine from the rear axles more easily.

Jonathan and I also spent about an hour fixing the VDO clock which tends to die on most 914s. It looked like the entire clock gear mechanism was intact but the motor wasn't turning. After playing with my new $400 oscope, I reverse engineered the crystal-driven circuit on the board and found an open capacitor. The existing capacitor was rated to 16 volts and probably exceeded its expected operating life of ten years or so running continuously in the car. I replaced it with a much more robust tantalum capacitor rated at 35 volts and the clocks runs fine now. Craig at Camp914 was gracious enough to give me an accessory bulb socket so I could light up the clock too.

This will probably be my last weekend of joyriding in the car in its gasoline form since Alan at A & P will be swapping out the suspension next Thursday. Things are starting to move forward.